Home > Jeep > 2000 Cherokee > Suspension Lift Kit Last Updated: 3.5.2006
The XJ Files

The Nitty Gritty:

Advantages of Upgrade:
Increased shock travel and ground clearance
Increased angle of approach, break-over angle, and angle of departure
Room for bigger tires
Looks more like a Jeep and less like a tall Volvo station wagon

Disadvantages of Upgrade:
Potentially causes steering and alignment problems
Higher center of gravity
Increased driveline wear
The first step into a seemingly bottomless money pit

Technical Specifications:
Rusty's Offroad 6.5" long travel kit
Includes front coils, rear leaf packs, leaf spring shims and Monroe shocks
Stainless steel brake line extensions
Replacement transfer case crossmember with lower control arm mounts
Fully adjustable upper and lower control arms
Fully adjustable track bar and heavy duty frame bracket

Tools Needed:
Various SAE and Metric sockets, allen bits and wrenches
Drill with standard, metric and hole cutting bits
Impact wrench
Floor jack, jack stands and tire ramps
Various pliers
Angle grinder
Rotary tool (Dremel)
Die grinder (or a torch or plasma cutter)
Phillips head and flat head screwdrivers
A "cheater bar"

Materials Used:
Underbody rust inhibiting primer and spray paint
Brake fluid
Rusted bolt solvent (Liquid Wrench, PB Blaster, WD-40, etc.)
Loc Tite (red and blue)
Various metric and standard hardware (The kit included the bare minimums. I replaced a lot of hardware out of necessity.)
Cutting wheels, grinding/sanding wheels and grinding bits

Final Cost:
Lift kit: $1600
Shackles: $150
Materials: $150 (mostly hardware and grinder bits/wheels)
Shipping (total): $277
Total: $2177

Project Overview:

A good suspension lift is the foundation of any better-than-stock offroad rig. A suspension lift lets you cram bigger tires under your Jeep (or ride of choice) for better traction and offers improved ground clearance, approach and departure angles, and break-over angle. Most other major mechanical modifications you make on a trail rig center around the lift.

Before
Before
After
After

Product Selection:

I struggled with this decision for a long time. I called around and did a lot of research before buying. In the end, there were four manufacturers I considered: Rubicon Express, Rock Krawler, Rusty's Offroad, and Clayton Offroad

I wanted a rear coil-over conversion kit from either Rock Krawler or Clayton Offroad, but I simply couldn't justify the extra $2,000 it would cost for one of those kits. I may consider that for future upgrades. But for now, this will do nicely.

Since I had ruled out a rear coil-over conversion because of cost, it really came down to features of the kit, cost, and installation. Ultimately, I chose the 6.5" long travel kit from Rusty's. It didn't require any welding to the unibody, which I preferred. (Not that I mind welding. And as it turns out, I had to do some anyway.)

Other Notes:

Lifting a Cherokee (or any vehicle) this much causes some unwanted side-effects. First, it introduces bump steer. It also introduces excessive driveline vibration because of the steep universal joint angles. To correct this, I installed a slip yoke eliminator and CV driveshaft.

As a reference, here are some measurements from before and after installing the lift.

Measurement Stock Lifted
Ground to wheel center (avg): 13.25" 16"
Ground to fender (avg): 30.5" 40.75"
Ground to front wheel center when flexed: 22.5" I need a forklift to find out!

One final note... The most valuable tool I had during this project was my 2.5' cheater bar. Some of the nuts and bolts were either torqued so tight or so corroded that it took me wailing on that thing to break them loose.

Installation:

Ground to fender height Before I started, I wanted to take a few measurements to reference once the lift was on. I measured the distance from the ground to the fender on all four wheels. Average was 30.5".
Ground to wheel center I also measured from the ground to the center of each wheel. Average was 13.25". Just by putting on 33" tires I lifted the Jeep by about 3". Add that to the 6.5" of lift from the kit and the Teraflex Revolver shackles and I should be about 9"-10" higher.
Jacking the front axle Next, I wanted to see how much "flex" I could get with the stock suspension, with both front and rear sway bars attached. I jacked up the left front wheel at the axle.
Front tire almost off the ground I jacked up the wheel until the right front tire started coming off the ground. You can see the tread is up off the ground just a little bit in this picture.
Full flex - stock As you can see in this photo, even a stock XJ with both sway bars attached has some decent flex. Once I had it jacked up as far as it would go, I measured the distance from the ground to the center of the axle: 22.5". That's 9.25" of flex from the stock suspension. You can actually get more flex when the suspension is "shocked," causing the sway bars to twist. But it's hard to measure anything other than static articulation.
Full flex - stock This is a good shot of how far off the ground the front tire can get off the ground with stock suspension. Good. But not good enough!
Rear tire stuffed - stock This photo shows how "stuffed" the rear tire is in the wheel well. I'll have some problems with tire rub once I put bigger tires on. Compare this photo to the action shot of my Jeep in "full flex" on the Upper Lopez trail.
Jack stands To begin, I jacked up one side at a time and put the Jeep on jack stands.
Jack stand placement I put one stand at each corner of the unibody frame. I wanted them to be spread out as much as possible to make it as stable as possible. I gave it a good shove test before I started doing any work on it. I was a bit paranoid about the thing coming down on me while I was working on it.
Front driveshaft removed Next, I removed the front driveshaft. (You can barely see it in the shadow of the Jeep, but it's there.) I did this so the front axle would be free to move, and also because it was necessary for my slip yoke eliminator installation.
Stock tires removed I got tired of working around the tires, so I took them off. In hindsight, I should have done this as soon as I had it up on the jack stands. But I was still a bit edgy about the thing coming down on me, so I wanted to leave the tires on. I got over it and just took the things off so I could work.
Rear sway bar With the tires out of the way, I removed the rear sway bar. It wouldn't be going back on later, so it went into the "E-bay pile."
Rear axle I then removed the rear driveshaft, disconnected the stock shocks from the axle and removed the U-bolts to free the rear axle from the springs. The rear driveshaft went in the sell pile. I also tried removing the stock shocks while I was under there. But, while trying to loosen the first bolt that holds the driver's side shock on, I sheered the head right off. That really ruined my afternoon, so I took a long break. I was not looking forward to having to drill that piece of crap out of there.
Rear axle removed Next, I installed the extended stainless steel brake line for the rear axle. Then I carefully lifted each end of the axle off of the jack stands (I needed them for my transfer case work) and set it on the ground. That allowed me to remove my springs. The bolts that held them in took a breaker bar with a 2.5' pipe on the end to break free, but I eventually got them off. I almost broke my 5" vice trying to loosen the bolts that held the shackles on. So I eventually gave up and ordered some Teraflex Revolver shackles instead. The stock springs and shackles went into the sell pile.
Transmission support To install the front suspension, I needed to remove the stock crossmember. The crossmember supports the weight of the tranny and transfer case. So, I put a jack stand under the transmission pan before I removed the crossmember. (This photo actually shows the crossmember already removed.)
Cut off bolt There are four nuts that fix the transmission to the crossmember. Then there's a bolt and a nut (on a stud fixed to the frame) on each side (end) of the crossmember that hold it to the frame. The driver's side nut and bolt came off easily. So did the passenger side nut. And, I thought the bolt did too - until I realized it was just spinning in its hole. The welded nut on the inside of the frame broke loose. There was no way to reach it to hold it in place to remove the bolt, so I had to cut the bolt head off. I would have to find a solution to the loose nut inside the frame later when I installed the new brackets for the lower control arms.
Broken bolts I finally stopped procrastinating and got around to removing the remaining bolts that hold the upper shock pins in on the rear shocks. Well, at least that was the plan. I sheared not one, not two, not even three, but all four of the bolt heads off! What a pain!
Metal shavings After shearing off all four bolt heads, it was time to extract the broken bolts. Again, that was the plan. After trying both left-hand thread and straight flute bolt extractors of various sizes, I eventually just drilled out each bolt completely. I was left with a lot of metal shavings on and around my rear axle. I vacuumed it up as soon as I could to keep from getting it in anything.
Tapped holes I used a thread gage on what was left of the thread on the head of one of the bolts to see what size bolt it was. Based on that, I tapped each hole with a 5/16-18 tap. I threaded a bolt into each hole to make sure they all threaded properly.
Front shock pin bolts To hopefully alleviate any similar problems on the front shocks, I soaked the front shock pin bolts with PB Blaster to loosen them up. Considering I did the same thing to the rear bolts, I wasn't hopeful. But it was worth a shot. I was in a bit of hurry to beat sunset when I took this picture, and my camera focused on the steering knuckle instead of the shock mount. You get the idea though.
Spring comparison As a comparison, here's what the 6.5" spring from Rusty's looks like compared to the stock spring.
Shock comparison Another comparison of the stock shock length to the Monroe shock that came in the Rusty's Offroad kit. I fiddled around briefly with the bushings and pins. I could tell it was going to be a royal pain in the butt to get those things put together.
Spring droop As soon as my new Teraflex Revolver shackles arrived in the mail, I installed my rear springs. Stock shackles are 31/8" from eye to eye. Collapsed, the Revolvers are 51/8". Extended, they're 101/2"! That's 53/8" of droop just from these shackles! You can see how low the springs are hanging. Re-installing the axle and getting the tires on was going to be a challenge.
Axle shims With the springs suspended from the frame, I replaced the axle locating pin with a longer one and installed the axle shims. These shims keep your differential pinion point up towards the transfer case to reduce driveline vibration.
Tight e-brake line I installed the driver's side U-bolts first. I couldn't get one of the U-bolts into the passenger side because the axle was still on the ground and the shock mount was at an awkward angle. Once I had the U-bolts in, I tightened them just enough to draw the axle up so the perch was flush with the shim. The emergency brake line was pretty tight. There was still a bit of play in it, but not enough to make me comfortable. I later decided that instead of replacing the brake lines, I would simply move the splitter bracket back a few inches. There was enough slack in the line between the e-brake lever and splitter bracket to do it easily.
Creative jacking To get the passenger's side U-bolts in (one of them, anyway) I had to raise the axle. But now, I was lifting the combined weight of the axle and the spring and compressing the spring slightly. Too much to do by hand. But the axle was too low to get my jack underneath. So, I raised the jack high enough to go over the axle and then used a ratchet strap to pull up the axle. I brought it up just enough to get the U-bolt in. Once I had the last U-bolt in place, I tightened all the U-bolt nuts on both springs and removed the jack. You can see how far up the pinion yoke is pointing. That's from a combination of the shims and the severe droop from both Teraflex Revolvers being completely extended.
Raising the rear axle I was now faced with the problem of getting tires back onto the rear axle. The combination of the taller springs and extended Teraflex Revolver shackles left my rear axle sitting on the ground, even though I had jacked up the Jeep more than eight inches. I couldn't just jack up one side and put on a tire because it started to lift the Jeep off of the jack stands. Not good. So I started by collapsing the Revolver shackles as much as possible and holding them closed with ratchet straps. That lifted the axle up about three inches. Then I installed the driveshaft into the pinion yoke.
Rear driveshaft installed I then reconnected the driveshaft to the transfer case yoke. It's a bit tricky to get it into the yoke, stretch it enough to seat, and tighten all the bolts all at the same time. This project would definitely be a lot easier on a lift.
Crossmember replaced To put tires on the rear axle, I would have to be able to raise one side at a time. I couldn't do that while the front end was still on jack stands. So I decided to put the tires back on the front. But, to lower the front, I would have to remove the jack stand holding up the transmission and transfer case too. So I had to re-install the stock crossmember. I didn't tighten it to specs or put the nuts on the studs that fix the transmission to the crossmember. I just needed it on there to support the weight of the tranny and T/C.
Stock front tires replaced I then replaced the stock front tires. Again, I didn't torque anything to spec. I just put them on tight enough to hold the wheels on nice and tight.
Raising the rear axle Then I jacked up the front end enough to remove the jack stands and then lowered the front end back down onto the tires. That allowed me to jack up one side of the rear axle at a time. As I raised each side of the rear axle, I placed a jack stand under it. Also notice that I chocked the front tire. Since the front driveshaft was still removed, there was nothing to keep the Jeep from rolling away while I was jacking and lifting.
Stock rear tires replaced I raised the rear axle just high enough to put the stock tires back on. I did that so I could then raise each side even further to put on the new tires. I was a lot more comfortable with doing all of this jacking with the Jeep resting on its tires. No way of it falling off a jack stand that way!
Rear tires installed I put on the new tires on the rear axle. Holy cow! That thing is high up! I couldn't wait to get the front done. Having the rear end back on tires made the rest of the project easier because I could use the e-brake to keep from rolling, it was higher (and easier to get under), and I could jack up one side at a time without worrying about it falling off jack stands. The downside was that my jack stands weren't tall enough to reach the frame and get the Jeep level, so I faced a similar jacking rodeo later on for my front axle.
Rear shocks installed Next I installed the rear shocks. Getting the bushings with the pins through them (at the top of the shock) through the shock eyes is a lot harder than it seems. To get them in there, I put them in boiling water for a while first to soften them up as much as possible. Then I liberally doused them with WD-40. Then, I used a deep socket to fit over the pin and pushed the bushing through.
Welding in a new nut Since the weld nut inside the frame broke loose when I was removing the stock cross member, I had to do something about it. I used a stepped drill bit (Uni-bit) to drill out the hole where it used to be. I drilled it big enough for a flanged nut to fit flush with the surface. Then I used a long bolt to hold the nut in place while I tacked welded it in place. Once it was in place, I removed the bolt and welded it all the way around. Once it cooled a bit, I ground off the excess weld, then primed and painted it.
One inch holes in frame To install Rusty's kit, you have to drill or cut 1" holes on the inside of the frame rails. I used a stepped drill bit to drill holes on the left side of the frame. But the right side is a really tight fit if you don't want to remove the exhaust (which I didn't). You could use a torch or a plasma cutter, but I don't have either. So instead, I used a die grinder with a rasp bit (actually 4) to "hog out" the holes. I also had to use the grinder to clean up the holes on the left side too.
New crossmember in place I would imagine that watching me install the new crossmember and frame plates was a bit of a circus act. But after much sweating and swearing, I got it installed. Rusty's actually sent me the wrong transmission mount initially, and it took me a day to figure it out. They sent one overnight to me, but the delay was very frustrating, especially after trying all day to get the one they sent me to work.
Coils removed Next I removed the stock front coils. To make it easier, I put the coil compressors on first and then lowered the axle down to the ground, just on the side that I was working on. That made it easier to get the coil off because I didn't have to compress it as far to get it out.
Coil comparison Here are the stock and new coils side-by-side. The new coil isn't actually 6.5" taller than the stock unit. However, it's a lot "beefier," which means it won't sag as much under the weight of the Jeep. Unfortunately, it also means I'll have a slightly harsher ride now.
Extended front brake lines With the coils out of the way, I installed the new braided brake lines. Don't forget to get the brass bushings off of the banjo bolt that threads into the brake caliper. The cable clamps that came with the new lines wouldn't fit on the bolt that the stock lines used to hold them in place. So, I either had to drill the holes slightly larger on the clamps, or drill and tap a smaller hole in the frame and get some hardware to fit it.
Track bar adjustment Since the axle was going to be so much lower, I needed to adjust the steering linkage by making it longer. If you don't make it longer then your steering wheel will be turned to the right when your tires are straight. I extended the track bar as much as I could with full thread engagement. If it's not enough to align the tires to the steering wheel, I would have to buy a drop pitman arm.
Lower control arms removed Next I removed the lower control arms. This is another task that would be much easier on a lift. It's hard to get a wrench on some of the nuts and bolts, and you can't get much swing with a breaker bar because you're sandwiched between the ground and the frame. Time and patience.
Upper control arms removed After the lower arms were out, I removed the upper control arms. The bolts at both ends are supposed to lock against the frame or the control arm itself to keep it from spinning. However, I had to use some locking pliers to hold some of them in place.
LCA brackets cut off Next came the tedious and extremely dirty task of cutting off the stock lower control arm brackets. I tried a reciprocating saw, wheel cutter and angle grinder (with a cutting wheel). Out of all of them, the angle grinder worked best by far. I went through 4 cutting discs, but I got it done. By the end, I and everything around me was covered in ultra-fine metal dust. Not a friendly thing to have in a mechanical project. I was so miserable (sweat + metal grit = uncomfortable) that I stopped to take a shower and get all the grit off. My daughter said I looked like I had beard stubble all over my face.
New paint and control arms Once the brackets were removed, I ground them smooth and painted and primed them. Nothing fancy. Just enough to keep them from rusting. Then I installed the new upper and lower control arms. To get the LCAs in, I had to remove the jack stands near the front wheel well. I had to locate them to the front of the frame, which is higher than the middle section. To compensate for the distance, I used some wheel ramps to set the jack stands on. Not pretty, but it worked.
UCA hardware According the the instructions that came with Rusty's kit (which I was learning weren't altogether accurate at all times), you need to reuse the hardware for the UCAs. However, as I stated before, they have brackets welded to them to keep them from spinning. But since the design of the new UCAs is different, the stock hardware wouldn't work. So I had to make yet another trip to the hardware store to get some new bolts, locking nuts and washers.
Checking axle movement After installing the new hardware for the UCAs, I used my jack to cycle the front axle all the way up and down. I had to adjust both brake lines slightly, but other than that there were no problems. The control arms pull up all the way to the frame when the axle is on the bump stop.
Front axle on the ground To make installing the new shocks easier, I dropped the front axle all the way onto the ground.
New shocks installed Putting the axle on the ground proved to be very benificial. The new shocks are ultra beefy, and compressing them a lot with the spring compressor would have been difficult. I was able to get them in easily with only a little bit of spring compression. I had about 2" between the upper mount and the top of the coil.
Front axle raised With both coils in place, I raised the front axle back up just to the point where the coils engaged at both ends. I didn't want to take the weight off of the jack stands just yet.
Installing shock bushings Again, I had to fit some bushings with pins into the new shocks. Using some big sockets and my vice made it easier, but certainly not easy. It's still a pain.
Front shocks installed After getting the bushings into the shock eyes, I installed the shocks. Notice that the brake line loop bracket is still loose in this picture. I later tried to drill the hole bigger so I could fit the stock mounting bolt through them, but the drill bit tore the thin aluminum to shreds. So I ended up just using some strong adhesive-backed cable clips.
Disconnects attached to sway bar Next I mounted the JKS Quicker Disconnects to the sway bar and installed the mounting pins on the axle. The stock bolts are pressed into the bracket, so I used a gear puller to push them back out. I had to disconnect the steering stabilizer shock to get the gear puller in to remove the passenger side bolt. I didn't adjust the length of the disconnects yet because the axle was still not in its final position.
Stock tires replaced With everything in place inside the wheel well, I put the stock tires back on. That allowed me to get the weight of the Jeep onto the axle, rather than on the frame, with the least amount of axle articulation.
New tires installed I then immediately installed the new front tires. Now the Jeep was resting completely on its tires and I was able to remove all of the jack stands.
Disconnects adjusted and track bar bracket installed At this point I was having a hard time staying focused! Seeing my Jeep up on all four new tires - finally - was exciting. With the Jeep resting on its tires, I was now able to adjust the JKS Quicker Disconnects to their final length. I also installed the new track bar bracket to the frame. It was really nice to be able to work under the front end without a bunch of jack stands in the way!
Axle off center It's difficult to see in this picture, but the axle was off-center by about 2" to the passenger's side. Installing the track bar later would correct this problem.
Front driveshaft replaced Before centering the axle, I replaced the front driveshaft and torqued it to spec.
Track bar installed Next I installed the new adjustable track bar. The track bar can be lengthened to accomodate more lift later. But for the amount of lift I was putting on, the shortest length is what I needed. I also aligned the tires to the steering wheel. I had lengthened the steering linkage considerably early. More than I needed. So I shortened it back up a bit until the steering wheel and tires were aligned. I still needed to get it professionally aligned, but this was good enough to get me back on (and off!) the road.
All done!! Wow! Finally done!! At this point I torqued everything to spec and double checked everything. I bled the brakes, greased all the fittings and filled the transfer case. I also had to recharge the battery because I left the door open and the ignition on (to unlock the steering wheel) for a while. Flex test and measurements next!!
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